Between June 1985 and June 2002, operators of Boeing aircraft made a total of 67 reports to Boeing of heater ribbon failures where thermal degradation was evident. Charred insulation material was identified in many of the reports, and structural damage from fire had occurred in at least two cases. In some instances, water had leaked from melted water lines, which, in one case, led to failure of an engine indication and crew alerting system (EICAS) computer.
Service Difficulty Reports USA 1999042300717, USA 1988040800197, AUS 19990967, and AUS 19991248 all reported burned heater ribbons. Two of the reports involved Boeing 767 aircraft and two involved Boeing 747 aircraft.
In addition to the fire damage associated with the occurrence flight, TSB investigators found a burned Cox & Company heater ribbon, protective tape, and Rubatex foam insulation behind the aft wall of the aft cargo area on the occurrence aircraft (see Photo 5). Although a self-propagating fire had not occurred, the area had become hot enough to burn through the Rubatex foam insulation and a nearby plastic clamp.
On 24 September 1992, Boeing issued SB 767-30-0024, which specifically addressed an overheat problem with the B241 heater ribbon installation on certain 767 model aircraft. The existing spiral-wrapped heater ribbon rated at 24 watts per foot was continuously activated. Boeing recognized that if the heater ribbon was powered while no water was in the water fill line, overheating of the heater ribbon could occur resulting in the heater ribbon, adjacent insulation blankets, and any debris being scorched. The SB called for the replacement of the existing heater ribbon with a thermostatically controlled, 7-watt-per-foot, longitudinally installed heater ribbon. C-GHML was one of the affected 767 models, but neither the previous operator nor Air Canada complied with the SB.6 Following this occurrence, a new Cox & Company 24-watt-per-foot heater ribbon was installed. The heater ribbon was spiral wrapped, a thermostat was not installed, and an insulating jacket was included. The jacket was an insulation blanket assembly that was wrapped around the water fill line and heater ribbon, and secured with a hook-and-loop fastener system.
On 20 October 2002, while checking the heater ribbons on C-GHML prior to the winter season, heater ribbon B241 was found to have overheated and the insulating jacket was burned. The heater ribbon was completely destroyed during the overheat condition. The insulating jacket was charred on the inside and discoloured from overheating on the outside. There was no other damage to the aircraft or surrounding materials. This particular heater ribbon had only been in service for three months.
Another Air Canada Boeing 767-300 aircraft was examined by TSB investigators, and a burned Cox & Company heater ribbon was found in the vicinity of FS 1395. In this case, the water line was wrapped in a jacket that consisted of an insulation blanket covered on one side with PET and on the other side with Bradley BF-6620, a polymer coated fabric. The jacket was held in place with a hook-and-loop fastener system similar to Velcro. The failure had burned a hole through the jacket. Further examination of the same aircraft revealed another overheated Cox & Company heater ribbon behind a sidewall panel in the aft cargo compartment near FS 1460.
Air Canada conducted an inspection of its fleet of 55 Boeing 767-200 and 767-300 aircraft. Numerous occurrences of overheated and/or burned heater ribbons were found in both visually accessible areas and hidden areas, such as behind wall and floor panels. Thirty of the aircraft were found to have defective heater ribbons (including both Cox & Company and Electrofilm brand), resulting in 66 ribbons being either removed or de-activated.
On 20 December 2002, while passengers were boarding C-GAVA, another Air Canada 767 aircraft, smoke was seen coming from the aft galley. The problem was traced to the B195 heater ribbon on the aft galley drain line P/N 417T2004-13. The heater ribbon, a vinyl Cox & Company brand heater ribbon, was completely destroyed during the overheat condition. The jacket was charred on the inside and discoloured from overheating on the outside. There was no other damage to the aircraft or surrounding materials.
There is little industry guidance available to quantify the effects of blanket contamination. According to documentation from various sources indicated in this section of the report, the flammability characteristics of materials can degrade in service when they are exposed to contaminants such as dust, lint, adhesives, grease, oil, or corrosion inhibitors. The aviation industry has yet to quantify the impact of contamination on the continuing airworthiness of insulation blankets. However, as this section of the report shows, there is a definite connection between contamination and flammability.
Various types of thermal acoustic insulation blankets have fuelled aircraft fires on several occasions. For example, a Lan Chile Airlines aircraft (Miami, Florida, B767-375ER, 28 January 2002) had a fire in the forward (lower) cargo compartment that was fuelled by contaminated insulation blankets. These insulation blankets showed significant signs of contamination and wear.
In 1991, following an occurrence involving a fire in a Lockheed L1011 (TSB report A91A0053), the TSB issued a Safety Advisory (A910106) concerning the fire hazard associated with lint accumulation. The Advisory suggested that Transport Canada (TC) notify maintenance inspectors and operators of transport category aircraft of the fire hazard, and require that maintenance procedures be amended as required to ensure inspection and cleaning of areas where lint and debris can accumulate. In response, TC issued Service Difficulty Advisory AV-92-04 on 10 April 1992, which, in part, recommended that, whenever planned inspections allow, an inspection be carried out for accumulation of lint, dust and cabin debris, and that visible accumulations be cleaned out to remove the fire hazards.
In the United States, the NTSB issued recommendations A-91-71 and A-91-72 to address the safety deficiencies identified in the TSB occurrence investigation. The NTSB recommended that the FAA notify principal maintenance inspectors (PMIs) and operators of transport category aircraft of the fire hazard posed by accumulations of lint and other debris on wire bundles. It was also recommended that the FAA require transport category aircraft manufacturers and airlines to amend maintenance manuals as necessary, to ensure thorough inspection and cleaning of areas where lint and other debris may accumulate and pose a potential fire hazard. In response to the recommendations, the FAA issued an airworthiness inspector's handbook bulletin entitled, "Origin and Propagation of Inaccessible Aircraft Fire Under In-flight Airflow Conditions." The Bulletin provides information on the potential safety hazard applicable to all transport category aircraft from the accumulation of lint and other debris on wire bundles. It also requests that PMIs disseminate this information to all operators of transport category aircraft and review their operators' maintenance programs to ensure that they include an inspection of aircraft wiring and removal of contaminants, especially in inaccessible areas.
In March 1998, as a result of a fire in a cargo compartment of a 747-200 freighter, Boeing issued Service Letters (e.g. 767-SL-25-084, 747-SL-25-170) for all its aircraft models (per Multi-Model Service-Related Problem 25-0103). An investigation by Boeing had revealed that the presence of corrosion inhibiting compounds may have contributed to the fire and could have been the reason the fire was not self-extinguishing. The investigation also looked at the accumulation of dust, lint, and other debris on the insulation blankets outside of the passenger/cargo compartment, and concluded that it was conceivable that a large buildup of contaminants on these blankets could ignite as a result of a high-temperature source. The Service Letters informed operators that applicable Boeing manuals would be revised to address the effects of corrosion inhibiting compound and other materials on the flammability of aircraft insulation blankets. They also informed operators that Boeing would provide presentations on this subject at future airline conferences to increase airline awareness. Operators were advised to remove foreign materials and to increase attention to periodic inspections and cleaning of the aircraft during maintenance to avoid blanket contamination.
In relation to the Swissair 111 accident investigation (TSB report A98H0003), the TSB issued safety recommendations concerning flammability test criteria (A99-07 and A99-08) and material flammability standards (A01-02 to A01-04). The fire hazards associated with contaminated insulation materials, dust, lint, or debris were not an issue in that investigation.
On 28 September 2000, the FAA issued Flight Standards Information Bulletin for Airworthiness (FSAW) 00-09 entitled "Special Emphasis Inspection on Contamination of Thermal/Acoustic Insulation." Also, on 08 November 2001, TC published Maintenance Staff Instruction (MSI) 42, "Procedures for the Inspection of Thermal/Acoustic Insulation During Heavy Maintenance Checks for Contamination," which reflected the FAA requirements of FSAW 00-09. Recognizing that the flammability of most materials can change if the materials are contaminated and that contamination may be in the form of lint, dust, grease, etc., all of which can increase the material's susceptibility to ignition and flame propagation, the FSAW and MSI require specific action on the part of PMIs with responsibility for 14 Code of Federal Regulations (U.S.) parts 121 and 125 operators. PMIs should ensure that the operator has established procedures in their approved maintenance program for the inspection of contamination on thermal/acoustic insulation during heavy maintenance checks. If the operator discovers contamination of the insulation, the operator should take corrective action, cleaning or replacing the insulation as appropriate. However, as evidenced by the recent Air Canada and Lan Chile 767 cargo area fires, blanket contamination has persisted.
TC raised the issue of contamination at the International Aircraft Materials Fire Test Working Group, and a task group has been formed to address this issue.
During the inspection of the occurrence aircraft, the TSB found significant contamination of the insulation blankets throughout the cargo compartments, including the areas behind the sidewalls and in the belly of the aircraft. This contamination consisted of soiled insulation blankets and large accumulations of lint, dust and other flammable debris. In the forward cargo compartment, numerous insulation blankets were incorrectly installed, were ripped and torn, or not installed at all. Furthermore, there were unapproved blanket assemblies in the forward cargo compartment. These included blanket assemblies with Douglas Material Specifications numbers and blanket assemblies of unknown origin.
The inspection of the occurrence aircraft and other 767 aircraft showed the existence of contaminated insulation blankets and debris in many cargo compartments with open floors. A considerable amount of blanket contamination in the form of dust, dirt, and lint was found under and behind panels in areas that are not readily accessible without the removal of panels. Subsequent to the occurrence, Air Canada examined the open forward and aft cargo areas of its 767 aircraft. A general clean-up of debris found in these areas was carried out. This action did not fully address contaminated blankets.
Regulations require that electrical wires and cables be protected from an over-current condition. Typically, a circuit protection device (CPD) is used to provide this defence. CPDs are designed to protect the wire or cable; they are not designed to protect the associated electrical components, such as heater ribbons or line replaceable units, which may require their own internal CPDs.
The majority of CPDs used in aerospace applications are resettable, thermal circuit breakers (CBs), developed as a replacement for fuses. These conventional CBs typically contain a circuit consisting of a bimetallic element and two electrical contacts, one of which is spring-loaded. When an over-current condition occurs, the circuit heats as a function of current flow and time. When the heat exceeds a preset amount, the bimetallic element bends, causing the spring-loaded contact to trip and open the circuit. The design is known as a "trip-free" CB, in that it cannot be reset in the presence of an over-current condition. After a predetermined interval for cooling, the CB is capable of being manually reset.
This type of CB has proven to be effective in accomplishing its primary role, which is to protect wire and cable from damage due to an over-current condition. Specifically, this type of CB successfully protects the circuit when the temperature and time duration characteristics of the over-current condition are within the CB's design limits.
However, some types of wire and cable failures involve arc faults. Arc faults can create circumstances that do not fall within the design limits of the over-current/time protection curve of conventional CBs. One such phenomenon is an intermittent metal-to-metal event (conductor-to-conductor or conductor-to-frame) known as a "ticking fault." Such events can generate extremely high temperatures at the location of the insulation failure; however, the current draw may not be sufficient to heat the bimetal element to the temperature necessary to cause the CB to trip.
In some cases, a breakdown of wire insulation can lead to other types of arc fault failures, such as arc tracking. The arc tracking phenomenon involves carbonization of the wire insulation material that can result in intermittent arc faults between conductors, or between a conductor and the aircraft or other grounded conducting material. Although the hazards created by ticking faults and electrical arc tracking are widely known, existing technology is such that there are no CPDs available for use in aircraft that can accurately and reliably detect faults associated with wire insulation breakdown. The U.S. Navy, the FAA, and aircraft manufacturers are sponsoring initiatives to address this shortfall in CPD technology. The goal is to develop an arc fault CB device appropriate for aircraft use.
Among the Civil Aviation Authorities (CAA), the FAA has traditionally taken a lead role in research and development to improve fire safety in aviation. In 1988, the U.S. Aviation Safety Research Act mandated the FAA to conduct fundamental research related to aircraft fire safety. The FARs are used internationally as the primary source for aircraft certification requirements, including material flammability standards. Current FAA regulations reflect a philosophy adopted following a study in 1975 to 1976, to determine the feasibility of, and the trade-offs between, two basic approaches to providing fire safety improvements to a modern, wide-bodied transport aircraft fuselage. The purpose of the study was to examine the impact of in-flight, post-crash, and ramp fires on fuselage compartments, and to assess the fire protection requirements.
The first approach looked at the potential of applying the latest available technologies in early-warning fire detection and fire extinguishing systems. This approach would involve what was described as a "fire management system," i.e. one that would incorporate fire detection, monitoring, and suppression throughout the aircraft. The second approach looked at the potential for improving the flammability standards of materials to be used in cabin interiors so that they would have high fire-retardant qualities and low emissions of smoke and toxic gas. The study concluded that there were merits and limitations to each approach, and that an approach combining a fire management system with selective material improvements may offer the most potential for providing timely fire protection in all cases.
Subsequently, as recommended in the FAA's Special Aviation Fire and Explosion Reduction Advisory Committee report, FAA-ASF-80-4, dated 1980, the FAA's main research and development efforts were directed toward what was determined to be the greatest threat: a post-crash fire. The post-crash fire scenario that was envisioned was an intact fuselage adjacent to a fire being sustained by uncontained aviation fuel. It was determined that the most significant threat to surviving passengers in such a scenario would be from burning cabin interior materials. FAA research concluded that in such a scenario, surviving passengers could become incapacitated owing to toxic gases generated by a phenomenon known as "flashover." Therefore, to increase survivability, the FAA concentrated its efforts on improving the flammability standards for cabin interior materials to delay the onset of flashover.
In-flight fires were considered to be rare, and the FAA concluded that the best defence against them would be through the use of cabin materials that had high fire-containment and ignition-resistance properties, and through the use of fire-detection and suppression devices in potential fire zones.
Research and development related to in-flight fires has led to increased fire protection in areas such as cargo compartments and lavatories.
As part of the FAA aircraft certification process, materials to be used in the construction of aircraft are required to meet specified performance (test) criteria or standards when exposed to heat or flame. These flammability test criteria are designed, in principle, to expose a given material to a representative in-service fire environment. When deciding on the type and amount of testing for a particular material, assessments are made of the composition of the material, the quantity to be used, and its location within the aircraft. The testing is designed to measure the tendency of each material to ignite and propagate a flame.
For the majority of materials used in the pressure vessel, the flammability tests in place at the time the Boeing 767 was certified consisted primarily of a variety of Bunsen burner tests. A single Bunsen burner was used as the ignition source. Each test could be varied in several ways. For example, the orientation of the material to the flame could be varied from the horizontal through to the vertical, the orientation being specific to the test objectives, which were based on the perceived threat. The vertical burn test would normally be the most severe. Also, the length of time that the material was exposed to the flame could be varied. A longer exposure time would normally equate to a more severe test.
For each of the various Bunsen burner tests, requirements were established to differentiate between a pass or a fail for the material being tested, the performance of the material being averaged over a minimum of three test specimens. The following is a list of criteria that could be used to measure a material's flammability characteristics:
Except for selected materials in Class C cargo compartments, the most stringent material flammability standards were applied to those materials that were to be used in the occupied areas of the aircraft. Of particular interest were large surface panels such as sidewalls, ceilings, stowage bins, and partitions. Not only were the materials used in the panels subjected to the most aggressive test procedures, the materials also had to be self-extinguishing, i.e. they would not propagate flame beyond a certain distance, typically less than 20 cm (8 inches). Cabin materials were also subjected to tests for heat release and smoke. No testing was required for toxicity.
As a consequence of the testing requirements, less stringent material flammability standards were applied to those materials intended for use within the pressure vessel but that were outside the occupied areas. Certain materials only required the horizontal Bunsen burner test. To pass, the material could not exceed a certain rate of burn. Depending on the intended use of the material, the rate of burn could not exceed either 6 or 10 cm (2.4 or 4 inches) per minute. No requirement existed for these materials to be self-extinguishing.
In effect, the different flammability testing requirements, as described above, resulted in the following material flammability hierarchy:
Therefore, many aircraft materials were certified even though they were either flammable or would burn within established performance criteria.
Many materials are installed in aircraft as part of a system, even though they are normally tested individually for flammability. For example, thermal acoustic insulation materials are typically installed as a system that includes cover material, insulation, and related components such as splicing tape, fasteners, and breathers. However, by regulation, the testing of the finished product only consists of insulation and cover material together. Consequently, the as-installed thermal acoustic insulation materials may pose a different propensity to ignite and propagate fire than its testing would reveal.
The process of importing an aircraft into Canada is complex and entails a variety of detailed checks. The documents used for the importation of aeronautical products into Canada are ACPL No. 50 Canadian Type Certification - Import Aeronautical Products, dated 30 May 1996, and MSI 26, Importation of Aircraft. The detail and level to which an aircraft will be inspected is based on where the aircraft is being imported from and the type of aircraft. In the case of C-GHML, the checks included a detailed inspection of the aircraft by the Triad International Maintenance Corporation while it was still in the United States, and a detailed examination of the aircraft records to ensure that all applicable standards of airworthiness had been complied with and the aircraft was in conformity with the type design.
The aircraft inspection produced a detailed list of 1959 deficiencies and maintenance tasks to be completed. Of particular note is the fact that every area of the aircraft was identified as requiring cleaning, but there were very few references to contaminated insulation blankets. Also, hundreds of discrepancies were noted within the forward and aft cargo compartments, including items such as missing light covers, the wrong type of lamp in a light fixture, and inoperable PDUs. Although the list was very detailed, the inspection failed to identify the unapproved insulation blankets in the forward cargo compartment.
Several factors led to the safe conclusion of Air Canada Flight 116 at its planned destination. The duration of the flight was approximately 5 hours and 21 minutes. The Master Warning Fire/Overheat light illuminated very near the end of the flight, 6 minutes and 24 seconds before the aircraft stopped on the runway. The aircraft fire detection and extinguishing system functioned properly, and the fire was effectively extinguished even though it was beginning to spread up behind the right sloping sidewall of the aircraft, outside the cargo compartment. The last line of defence, the compartment liner that was designed to contain the fire, had been breached. The fire spread and increased in intensity until it was successfully detected and extinguished by the on-board system. The primary factors involved in this occurrence include:
The analysis will look at these safety deficiencies and other aspects of the occurrence that, although not causal, present some degree of increased risk to aviation safety.
Early in the investigation, it became known that the source of ignition was the B110 heater ribbon laid longitudinally along the water supply line. The heater ribbon failed just aft of FS 1395, at a recent water line repair.
It is likely that the temporary repair to the water line resulted in dissimilar heat sinks that produced localized overheating of the heater ribbon, which was exacerbated by multiple layers of 3M 474 tape and Rubatex foam insulation. This localized overheating degraded the surrounding EPDM insulating matrix to the point where the heating elements arced and ignited the surrounding material. The failure continued until a conductive path was no longer available and the arcing ceased. The dissimilar heat sinks comprised the following: the original Teflon water line; the stainless steel clamps used to secure the repair in place; the stainless steel tube used for the repair; and the air gap created by the difference in diameters of the stainless steel tube and the original water line.
The water line to which the heater ribbon was attached was constructed of a Teflon tube with a braided Nylon outer sheath, neither of which are efficient conductors of heat. The stainless steel clamps and tube, on the other hand, were very efficient conductors of heat. The least efficient conductor of heat in this scenario was the air. Heat generated by the heater ribbon is absorbed in two ways. A portion of the heat generated is absorbed evenly along the length of the water line, and the remainder of the heat is dissipated evenly into the surrounding ambient air. The repair to the water line resulted in an uneven heat distribution and localized heating. The localized heating compounded by the layers of 3M 474 tape and Rubatex foam insulation raised the temperature above the design specifications of the heater ribbon, thereby allowing thermal degradation of the heater ribbon's insulating matrix and surrounding material. Degradation of the insulating matrix allowed the heating elements to migrate towards each other and eventually arc.
Circuit breakers (CBs) are designed to protect aircraft wiring from an over-current condition; however, not all electrical fault situations will cause a CB to open. The failure mode of the heater ribbon did not produce an over-current condition that would endanger the aircraft wiring or trip the CB. Once the fire was detected and the fire extinguishing system activated, it would be expected that power would be removed from all but the required essential systems as a means of eliminating potential ignition sources. This was not the case in the Boeing 767, nor is it a regulatory requirement. The heater ribbons remained powered throughout this entire event, and there was no means of deactivating them from the flight deck. As long as power is available to the heater ribbon, the potential for the heater ribbon to arc exists and presents an ongoing risk.
Research clearly indicates that heater ribbons have a propensity to fail and are replaced on a regular basis. It is also noted that the older style of vinyl-covered Cox & Company heater ribbons, with a lower continuous operating temperature, fail most frequently. Often, the failures go undetected for long periods of time and are not discovered until a major inspection, such as the yearly winterization check. The most common form of failure appears to be overheating, which often leads to the complete destruction of the heater ribbon. Some of the failures resulted in self-extinguishing fires. In most cases, the failed heater ribbons caused localized damage, which was easily repaired. In one instance, a failed heater ribbon melted a water line; water leaked from the line and resulted in the failure of an EICAS computer.
The Flight 116 occurrence showed that it is possible for a failed heater ribbon to ignite a self-propagating fire. It is also significant that, while the fire occurred in a sealed compartment with a fire extinguishing system, the fire had breached the cargo compartment and entered an inaccessible and unprotected area. Had the fire extinguishing system not extinguished the fire quickly, the results could have been catastrophic.
The procedures for the installation of heater ribbons were generic and often ambiguous. This led to difficulties and confusion in determining how a heater ribbon should be installed. The exact installation of each and every heater ribbon is critical, as an improper installation can result in an overheat condition that can lead to a fire. There should be no ambiguity in the installation instructions.
There also appears to be a general sense of complacency in the aviation industry with regard to heater ribbon failures. Personnel working in the industry have known for years that heater ribbons fail regularly. They are considered by most to be non-critical systems, the failure of which usually results in very little damage. It is not until a serious occurrence that the potential danger posed by a faulty heater ribbon is fully realized.
The above information concerning heater ribbon failures supports the existence of an unsafe condition relating to the potential for water line heater ribbon installations to provide a source of ignition, combined with the availability of flammable materials sufficiently close to the ignition source to ignite.
The most significant deficiency in the chain of events that resulted in the fire on C-GHML was the presence of flammable materials that allowed the fire to ignite and propagate. The PET covering material on the insulation blankets was contaminated and flammable. This was the most significant source of combustible materials that contributed to the fire. The PET-covered insulation blanket was also most likely the first material to ignite. Debris in the area of the fire damage was found to be combustible and was consumed as the fire progressed through the insulation blanket. This debris included paper, candy wrappers, Styrofoam packing peanuts, and small polyethylene beads that had collected in the bilge area.
Research clearly indicates that contamination in aircraft is an ongoing problem. Although many steps have been taken by the regulators, manufacturers, and operators to reduce the risk, contamination still exists. Open cargo floors in aircraft provide a gathering area for flammable debris to collect, but they also permit easy access for the clean-up of debris. Even though the debris can be easily cleaned, fluids of unknown flammability can leak from baggage and cargo and go undetected. Additionally, fluids used for cleaning and lubricating cargo compartment components during routine maintenance can also spill and go undetected. Of more concern are the areas that are not readily accessible. It is in these areas that heavy accumulations of dust, lint, and small flammable materials such as paper collect on insulation blankets, aircraft wiring, and electrical components. As well, fluids spilled from the passenger cabin, lavatories and galleys can leak into these areas. These areas are not easily accessible, have no protection from fire, and are usually only accessed every few years during heavy maintenance checks.
Inspection of the occurrence aircraft and other aircraft in the Air Canada fleet during the investigation showed heavy accumulations of dust and lint on insulation blankets and electrical components behind panels.
It is noted that little is known about how age and contamination affect the flammability of existing in-service materials. However, testing has indicated that materials that once passed old certification standards often do not pass current standards, and there is no requirement to replace most of these materials.
The drain line repair was most likely the catalyst that initiated the B110 heater ribbon failure. The drain line was repaired twice prior to the occurrence, under a repair scheme that was approved and issued by Air Canada's engineering department. The repair was meant to serve as a temporary fix until a new drain line could be installed. The repair was not authorized by Boeing, nor was Boeing's authorization required.
The first time the repair was carried out, the heater ribbon had failed and it was replaced. The second time the repair was carried out, the heater ribbon was not replaced. While carrying out the second drain line repair, the heater ribbon may have been inadvertently damaged; however, fire damage to the heater ribbon precluded the possibility of determining if this was the case.
The fact that a minor repair could possibly affect the serviceability of a component in such an adverse manner supports the need to carefully examine heater ribbon installations.
Prior to the aircraft entering Canada, it was inspected in accordance with existing procedures. The inspection was detailed and generated an extensive list of discrepancies and maintenance tasks to be completed. Eventually the aircraft was issued an Export Certificate of Airworthiness from a country with which Canada has a bilateral agreement (U.S.). This was accepted by the TC delegate assigned to the project.
Although the inspection was detailed and the reports generated did make reference to some discrepancies with the insulation blankets in the cargo holds, these references were not very detailed. It is possible that the unapproved blankets found during the investigation were missed during the importation process, or were noted during the process but, due to the lack of detail of some of the references, were not addressed prior to the aircraft entering the country. Regardless of how the aircraft was imported, it is the responsibility of the owner to maintain the aircraft in accordance with its type design certification. If the aircraft were dirty or there were unapproved insulation blankets installed, it was Air Canada's responsibility to rectify the problem.
The delay of the operator in notifying the TSB in a timely manner following the occurrence and the loss of flight recorder information did not adversely affect the investigation for the following reasons:
Notwithstanding, had the circumstances been different, the lack of data following the cargo fire or the delayed notification could have severely affected the ability of the investigation to make findings as to the causes and contributing factors.
Although NTSB Recommendation A-02-24, "Overwritten Cockpit Voice Recordings," was issued on 29 August 2002, implementation of the recommendation by the FAA would only affect aircraft operators certified to conduct operations in the United States.
Air Canada took immediate action to reduce the risk of heater ribbon fires. An inspection of specified areas of the 767 aircraft fleet was conducted, and defective heater ribbons in these areas were removed or de-activated and a general clean-up of debris found in these areas was carried out. Not all of the heater ribbons in the 767 aircraft were examined.
Air Canada amended its Boeing 767 Service Check (96-hour maximum interval) to include a requirement to remove all debris found below the floor level of both the forward and aft cargo compartments. They also enhanced their zonal general visual inspection to ensure that heater ribbons are inspected during the scheduled 24-month "M" checks.
Air Canada has initiated new procedures to ensure that the required flight recorder information is provided. For any given situation, there are several individuals within Air Canada who can request that a flight data recorder (FDR) or cockpit voice recorder (CVR) be quarantined, but only the Director of Flight Safety or a delegate has the authority to release flight recorder information and then only to the TSB.
As a result of the fire on aircraft C-GHML, Boeing released Alert Service Bulletin (ASB) 767-30A0037 on 28 May 2002, to provide instructions and corrective action necessary to avoid a possible fire in the forward and aft cargo areas. The bulletin is applicable to all 767-200, 300 and 300F aircraft with non-fully enclosed cargo floors in the lower cargo areas. The bulletin called for operators to take the following actions with respect to visually accessible potable water and drain lines located under the cargo floor in the forward and aft cargo areas:
In a letter dated 31 October 2003, Boeing provided additional information regarding TSB recommendations A02-04 and A02-05 (see Section 4.1.3)
On 14 November 2002, the TSB issued the following, regarding water line heater ribbon fires:
Widespread use of heater ribbons on transport category aircraft exposes the travelling public to the risks associated with heater ribbon fires. Recent actions taken to reduce these risks are not comprehensive and do not address the risk in the long term. Consequently, there remains inadequate defences against heater ribbon installations starting a fire, therefore the Board recommends that:
The Department of Transport take action to reduce the short term risk and eliminate the long term risk of heater ribbon installation failures starting fires, and coordinate and encourage a similar response from other appropriate regulatory authorities. (A02-04)
On 14 November 2002, the TSB issued the following recommendation covering contaminated, thermal acoustic insulation as a source of fuel:
The widespread existence of contaminated thermal acoustic insulation materials and debris on transport category aircraft exposes the travelling public to the risk of a self-propagating fire. Recent actions taken to reduce these risks are not comprehensive and do not adequately address risk in the long term. Consequently, there remains inadequate defences against contaminated insulation materials and debris propagating a fire, therefore the Board recommends that:
The Department of Transport take action to reduce the short term risk and eliminate the long term risk of contaminated insulation materials and debris propagating fires, and coordinate and encourage a similar response from other appropriate regulatory authorities. (A02-05)
On 07 June 2002, the FAA issued Airworthiness Directive (AD) 2002-11-11, which reflected Boeing's ASB 767-30A0037. The FAA indicated that action associated with the AD is considered interim until final action is identified, at which time the FAA may consider further rule-making.
In a letter dated 06 February 2003, the FAA's Seattle Aircraft Certification Office indicated that they agree in part with TSB Recommendation A02-04.
In a letter dated 19 March 2003, the FAA's Seattle Aircraft Certification Office indicated that they agree with TSB Recommendation A02-05.
Transport Canada (TC) responded to Recommendation A02-04 with the following action:
Short-term Actions
Long-term Actions
TC responded to Recommendation A02-05 with the following action:
Short-term Actions
Long-term Actions
The Board is concerned that the FAA action is limited to Boeing 747 and 767 aircraft, because only these Boeing aircraft have open cargo floor areas. The FAA believes that heater ribbons do not need to be removed or replaced in closed-in areas, because such areas do not accumulate sufficient debris and contamination to pose a risk of a self-sustaining fire. The Board does not share this view. Both the TSB and the National Transportation Safety Board (NTSB) have previously issued safety communications concerning the fire hazard associated with the accumulation of lint, dust, and debris on wires. As well, both TC and the FAA have previously issued communications recognizing that the flammability of most materials can change if the materials are contaminated, and that contamination may be in the form of lint, dust, grease, etc., which can increase the material's susceptibility to ignition and flame propagation. Despite all of the action taken to date by the various agencies, the problem of contamination in closed-in areas still exists (see photos 6 and 7). As detailed in this report, dust and lint accumulation on wires has led to self-sustaining fires in closed-in areas, and the potential for such fires still exists. Consequently, the lack of FAA action concerning closed-in areas does not mitigate the safety deficiency in these areas.
FAA action will likely adequately address the potential for heater ribbon installations to start a fire in open cargo floor areas, but not in closed-in areas. Although the risk of a fire starting in open floor areas is likely greater due to their vulnerability to the accumulation of debris and contamination, the risk of a fire starting in a closed-in area will remain.
The Board is concerned that although TC has indicated its intention to work with the FAA and has made requests to the FAA, TC has not indicated an intent to take action to directly address the safety deficiencies identified by the Board beyond the areas being addressed by the FAA.
This report concludes the Transportation Safety Board's investigation into this occurrence. Consequently, the Board authorized the release of this report on 26 August 2004.
The following TSB Engineering Laboratory reports were completed:
LP 35/02 - Cargo Fire Examination
LP 39/02 - FDR/CVR Analysis
LP 58/02 - Heat Testing of 3M Vinyl Tape-Flame Resistant-474
LP 106/02 - Water Line Ribbon Examination
These reports are available from the Transportation Safety Board of Canada upon request.
| ACPL | Aircraft Certification Policy Letter |
| ACPP | Air Canada Production Permit |
| AD | Airworthiness Directive |
| ASB | Alert Service Bulletin |
| ATPL | Airline Transport Pilot Licence |
| ATSRAC | Aging Transport Systems Rulemaking Advisory Committee |
| BL | buttock line |
| CAA | Civil Aviation Authorities |
| CARs | Canadian Aviation Regulations |
| CB | circuit breaker |
| cm | centimetre |
| CPD | circuit protection device |
| CVR | cockpit voice recorder |
| EICAS | engine indication and crew alerting system |
| EO | Engineering Order |
| EPDM | ethylene propylene diene terpolymer |
| EZAP | enhanced zonal analysis procedure |
| F | Fahrenheit |
| FAA | Federal Aviation Administration (U.S.) |
| FARs | Federal Aviation Regulations (U.S.) |
| FDR | flight data recorder |
| FLIR | forward-looking infrared |
| FOD | foreign object debris |
| FS | fuselage station |
| FSAW | Flight Standards Information Bulletin for Airworthiness |
| Hz | hertz |
| IFR | instrument flight rules |
| LBL | left buttock line |
| MSI | Maintenance Staff Instruction |
| NPRM | notice of proposed rule making |
| NTSB | National Transportation Safety Board |
| OM | Operations Manual |
| PDU | power drive unit |
| PET | polyethylene terephthalate |
| PMIs | principal maintenance inspectors |
| P/N | part number |
| RBL | right buttock line |
| SB | Service Bulletin |
| TC | Transport Canada |
| TSB | Transportation Safety Board of Canada |
| U.S. | United States |
| º | degree(s) |
1. All times are Coordinated Universal Time (eastern daylight time plus four hours).
2. See Glossary at Appendix B for all abbreviations and acronyms.
3. An aerospace term used to describe a reference line that runs along the length or the longitudinal axis of the aircraft. An aircraft contains several buttock line sections.
4. A squib is a small pyrotechnic used, in this case, as a means of activating the fire extinguishing system when selected by the crew.
5. Strong, coarse fabric used for heavy-duty lining to prevent shrinking, checking, etc.
6. There was no regulatory requirement to comply with SB 767-30-0024.